• 集群首页
  • 关于我们
  • 期刊群

文23枯竭砂岩型储气库微泡钻井液技术

Drilling fluid technology for the Wen-23 depleted sandstone gas storage

  • 摘要: 文23储气库是以巨厚盐层为盖层的枯竭砂岩气藏型储气库,具有地层孔隙度高、渗透率变化大、压力系数低、亏空严重等特点,钻井过程中井漏、地层污染等问题突出。为此,研发了发泡剂、稳泡剂,开发了抗温120 ℃防漏型低密度微泡钻井液体系。该体系在120 ℃条件下,经72 h老化后密度变化仅0.04 g/cm3,仅需325 mL承压即可达到10 MPa以上,对地层的渗透率恢复值达87.9%。微泡钻井液先后在文23储气库现场应用66口井,漏失发生率仅为13.6%,施工期间井壁稳定。抗温120 ℃防漏型低密度微泡钻井液在文23储气库建设中表现出了良好的防漏效果,同时有效地保障了井壁稳定,降低了储层伤害,为文23储气库安全、高效开发提供了有力技术保障。

     

    Abstract: The Wen-23 gas storage reservoir is a depleted sandstone type gas reservoir with a massive salt rock cover and a maximum temperature of 120°C at the bottom. To address severe leakage and formation contamination during drilling in the Wen23 reservoir, a leak-proof low-density micro-foam drilling fluid system with a temperature resistance of 120°C was developed. Test showed that the micro-foam drilling fluid system had a density change of only 0.04g/cm3 after 72hrs aging at 120°C. Only 325mL was required to reach a pressure of 10MPa or more with the permeability recovery value of the formation up to 87.9%. The micro-foam drilling fluid has been applied to 66 wells in the Wen-23 gas storage reservoir with the incidence of leakage only 13.6%, and the well wall was stable during the drilling operations. The leak-proof low-density microfoam drilling fluid with 120°C resistance has demonstrated good leak prevention in the construction of the Wen-23 gas storage reservoir with effective protection of the well wall stability and reduction of the damage to the reservoir, providing a guarantee for the safe and efficient development of the Wen23 gas storage reservoir.

     

/

返回文章
返回